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Well i promised an update on the '88 around Xmas, so here it is: First things first: Reinstalled the brake booster/master on firewall and then removed the steering column in trade for my original column. I also managed to find an 87-91 wheel w/o the cruise buttons which will be going on at a later date So, then this happened: Front clip + 42s back on!!! Truck is so big, the garage door wouldnt open if the hard top was on! The front clip was inevitable. I needed the 42s on though. Since i want it to be a bit more streetable, last year i bought a set of Bushwacker cut-out flares. But, i dont like the look of the 87-96 flares, so i bought 80-86 instead. Since they technically dont fit, i couldnt follow the directions to install them. So instead i needed the tires on the bronco so i could figure out where the flares actually need to go. So, here we go! I started at the rear left, because gas filler door. Cardboard mockup of sheetmetal to be removed: some rust thats gonna have to go: Bam! Flare mocked up! Its impossible to get good pics with this side against the wall. I have the filler door cut and sitting on my work bench, need to get that reinstalled. Passenger side installed! Looks good, i really like the shape of these flares They just barely cover the tires With the rear done, i can move on to the front: This shows the absolute minimal amount of sheetmetal you can remove to install the flares. Its mostly in the corners Flare mocked up The corner will get cut off, but not till way later down the road, when i get around to building a front bumper The money shot: This shows how much more material i can remove w/o impacting the install of the flare. More on this later. Driver-side cut Rust: repaired So, here's the plan. Once all 4 flares are 'installed', ill then remove them. Plan is to install riv-nuts in the fenders, and use machine screws to hold them in place. I want to be able to easily remove them when i go wheeling. Theyre too expensive to smash on a tree! So, back to these two pics: This actually looks like a pretty good amount of room for the 42s. Most of the clearance issues i ever had were at the corners anyway, not at the top. However, as you can see from this pic, theres lot of more sheet metal i can remove, and still be able to reinstall the flare: So the plan now is to open the wheel wells up a tad bit more, install riv-nuts and then weld them back together again. My goal is to have a nice open wheel well for wheeling, and then install the flares over top of them for when im not offroad. But before i can cut the wheel wells any further, i need to reinstall the fender liners, and see what i can get away with. Thats why im doing the front first; once i get a final shape to the fronts ill remove the rear flares and do the same. Then the flares can go back in their boxes, and the 42s can come back off, until way later down the road. So ive been thinking about the OBA on the 88. When i first put the 460 in, i put the York where the factory a/c compressor used to go. While this worked well, it caused problems with the factory air intake. I figured while the front clip is off, is the perfect time to come up with a better solution. Looking at it, there is definitely some room down where the smog pump used to be Problem is, it would require a ton of work to the bracket to get it in there. As it sits in that pic, its laying on the frame. I considered putting it where the alt was, and moving that down as it would be easier to do I rejected this idea as well, because i dont like having the alt down that low. So i pretty much had no choice but to see if i could build my own accessory drive bracket. So, here we go! With the stock bracket gone, there is a ton of room York mounting plate Making some spacers Main plate, roughly cut to size York hung, plenty of clearance to frame now: threading some bar stock Designing the alt mount. Reusing the bushing from the OEM alt mount Reusing the OEM tensioner bracket CAD (cardboard aided design) for the 2nd half of the alt mount Welding it all up final fit on the motor ...and all done & painted! Final install on engine: Its a tight fit, but it looks like its going to work well. This took me a while as the little guy consumes most of my free time these days, but it worked out well because it gave me time to stand back, take it slow and make sure nothing interferes with anything else. It goes together pretty easily, no bolts in awkward places or anything like that. Hopefully it works well, but the motor wont be running any time soon, so i guess we'll have to wait until later to see it in action!
Still sorting out the belt length; guessed wrong and got one this morning that ended up too short by an inch or so, gotta return it and get one a little longer sometime during the week. So a buddy found a Warn M12000 for sale on FB. Missing electronics, but at $500 still too good of a deal to pass up, so i ended up buying it last week. This thing is massive, it dwarfs my 8000Xi The M12000 is supposed to come with 3/8" cable, this one came with 7/16", which is what Warn used on the M15000 (15k winch) So i did some digging. Turns out this winch came off of a Dodge Powerwagon. It uses the 7/16" cable that the 15k winch uses, and the cable spools off the top of the drum instead of the bottom like the regualr 12k. Also, it uses the same planetary & all internal components of the 15k winch, which means that for all intents & purposes, this is a 15k winch! Apparently Warn sold Dodge a 15k, which was de-rated as a 12k, presumably due to liability issues. Once i get the front clip all done and back on the '88, ill have to build some kind of beefy bumper to carry this thing. 351 #2, all cleaned up, ready for install: Dropped the motor in friday morning after work: This motor came with all the parts for the OEM oil cooler, so thats on there as well. ...and the money shot, taken about an hour ago. She runs! 50 psi oil pressure cold, 25 warmed up. Drove it around the block for the 1st time earlier, motor feels strong. Its got a tick, i think its a lifter on the passenger head. Its not super loud, so im gonna run it and see if it gets quieter once i put some miles on it. Here's hoping this motor lasts longer than the last one! So! progress has been slow, but it has been made. Had some delays and other projects around the house to tend to, before i could really tear into this thing. So, here's what i found. So the verdict is in, the 351 is blown. Turns out when i cranked it over, i bent the #8 rod, and the crank hit the piston and broke it. Blown head gasket: One of 3 chunks that broke off piston Motor apart: Lots of metal in the pan patiently awaiting its demise Did some searching online, trying to figure out what to do. Rebuild, replace, used motor, etc. Ended up stumbling across another 351 with 70k on it for $400, so i snagged it up, and then sold an 8' truck bed i had kicking around, to cover the cost. ...and the donor 351, coincidentally also out of a 97 F250 Broke 10 of the manifold bolts. Extracted em all, and chased threads in every hole Degreasing Sloppy chain replaced This pretty much gets me to today. i snapped a bolt off for the water outlet, thats been removed and the threads chased. Also snapped one off in the timing cover, but that was fixed before i did the chain. So many broken bolts! Took forever to take care of them all. I am reusing the valve covers & oil pan off the original 351, but since they got all beat up pulling the motor, they got a fresh coat of paint this morning. I need to order a water pump and a couple other seals i dont have laying around, and then i can paint the block and begin putting the motor back together. My goal is to be able to drop the motor in the truck next weekend. The donor motor had the oem oil cooler on it, along with all the hoses. Im going to reinstall it, as soon as I source a replacement o-ring for the cooler adapter to the block as well. Left for work Saturday night, everything was fine. But when I went to leave Sunday morning it wouldn't start. Engine wouldn't turn over. Didn't sound right. Yanked the starter and a buddy/coworker brought me to Autozone to test it. It failed. Bought one and put it in. Engine stopped twice, then turned over and fired. Got out to listen, sounded like it was stumbling a little bit. Walked around to back and saw it dumped almost a gallon of coolant out the tailpipe: Shut it off. He drove me home, where another buddy/coworker met me. We hitched the trailer up to the diesel, unloaded it (its got a bronco top on it, plus an 8' bed), and drove back to work. So all said, I was gone about 2 hours. Couldn't get trailer to truck, had to start it. Same thing bumped it 3 times before it started. Didn't sound good. Moved it about 20' and shut it off. Positioned trailer and winched it up onto trailer. On ride home, had a blowout on trailer. Front right, never seen one go like this before I always carry 2 trailer spares so we pulled over, swapped it and got home. Unloaded truck in driveway, and used buddies jeep to pull off trailer, turn around, and then get into garage. Monday I drained cooling system. Only 1 gallon of coolant left. Drained and replaced oil, got about a quart of coolant out of pan. Pulled plugs, #8 had coolant on it. Cranked motor over to clear cylinders. Went to put plugs in, got to the last one, dropped it and broke it. Done for the day. This morning I got the last one in. Fired up motor. No serp belt on it so the water pump wouldnt pump fluid, and no lower rad hose hooked up either so cant run it for too long. Engine was hammering hard. So it looks like its gonna be coming out. So I figured since I have money & time invested in the engine & trans, I might as well get some gauges to monitor them. Enter a set of Autometer's GS gauges: Trans temp probe in the usual location; the test port Built a simple manifold to allow me to use both the stock pressure sender & the autometer oil pressure sender Working on the wiring harness. Since the GS series are LED, I have a resistor in-line to dim them a bit, so they match the dash brightness some wires poking out of the a-pillar... ...and gauges done! Looks like the motor is ~45 PSI cold, and never drops below 20 PSI even when hot @ idle. Haven't seen trans temps above 140º yet, altho I haven't driven it much since I finished em.
Been driving the hell out of this thing, so naturally the one thing I didn't touch would need work. I had this really neat noise under load (thinking going up hill), and then a rumble going down the other side of the hill (which sounded like it was coming from the rear axle). So I split the tcase open to inspect: the arm for the oil pump has worn a pretty deep groove into the tcase housing. it makes this cool (not really) rattly noise under load which sounds like bad bearings. Long story short, I stripped her clean Bought a bearing kit & a pump kit off ebay just in case. I changed all the bearings. Didn't really need the pump kit, but I used it anyway cuz I was already in there. Then welded a tab to the original arm, so it cant rattle around in there anymore. That's pretty much it. I didnt bother to take too many other pics, as there is already a great thread over on FSB of the full BW1356 rebuild, located here. Needless to say, the tcase is nice and quiet now. Well worth tearing into now, before the pump finally failed. Ok, here we go. So I got it on the road, and the trans was running great. I DD'ed it for about a week and a half, before I heard it. Going uphill under load (think freeway speeds) I started hearing a noise similar to that of an idler pulley that is about to explode. Which is what I thought it was, until I got to the top of the hill, then it went away. As I went down the other side, a vibration in the floorpan. Road levels out and its gone. Noticed it again a day later, again on my ride to work. Long story short I figured it out. Uphill, under load, 3rd or 4th, a tinny idler-about-to-explode sound. Coasting down the other side a vibration. Nothing in 1st or 2nd. Trans shifts great, converter locks up nicely. No codes, no burnt fluid, nothing. Unfortunately, or conveniently (depends on how you look at it), the rear main also sprung a leak. So the trans had to come out. Dropped the pan and found dark oil, and the typical amount of material, but nothing unusual. Keep in mind, I never changed the ATF, so this oil is many many years old I decided, what the hell. Stood the trans up and drained the rest of the oil out. With nothing usual seen from underneath, and no visible signs of a bad converter, I decided to pull the front pump out. I looked at it this way: I have a spare 2wd E4OD from the parts truck, so if I need to replace the converter or pump, ive got one. Front pump out: Decided to pull the O/D planetary and forward clutch out to inspect; thankfully everything looked great. ..but then.... ...wait a minute! What the F?! The O/D snap ring has come out????? So I did some research, and foud out that this is a known issue with the E4OD. The snap ring comes out of its groove, which takes the tension off the O/D clutch (AKA the O/D Apply Piston). Apparently it makes a funny noise, and if left unchecked, will burn up the OD clutch. Guess it was a good thing the rear main started leaking, cuz I think I just found my trans problem!!!! So cue this bad boy. its an upgraded snap ring made by Sonnax. It looks more like the snap rings that come with Warn hubs; it wraps around twice, and has locking tabs. This bad boy will never fall out. It is a PITA to install though, had to build a makeshift tool to compress the pressure plate so I could install it. ...and done! No way this thing is ever coming out on its own. I did take the time to examine all forward clutches (since I was already in there) and they all look brand new. So either this thing was babied its whole life, or it was previously rebuilt. Good deal. So I decided to take a look at the front pump. Stator support removed; pump case split in half. Check the inside! So then I figured, since its apart, I might as well throw Superior's Pump Correction package at it too! It comes with a couple new cup plugs, a new metal anti-drainback valve to replace the OEM plastic one, an upgraded front pump bushing, new front pump seal, and some scary directions. So lets get started! Step one is to knock out two cup plugs, drop in a new one, drop in this AL rod (to apparently block off an oil passage) and then a new cup plug behind it Open this orifice up to 3/32" Open this orifice to 3/32" Open this drainback port to 5/16" Drill a friggin 1/16" hole right thru the pump! Drill another 1/16" hole right thru the pump, into the oil passageway! On the stator support, remove the cup plug from the top hole. Its a blind hole; its gotta come out the way it goes in. I screwed a drill bit into it, and was able to pull it back out that way OEM plastic drainback valve on top, new metal one on bottom. this goes underneath the cup plug you just removed. If you overheat the trans this valve can melt, and when happens, goodbye O/D planetary/sprag. Upgraded pump bushing, with knurls to keep it from spinning in the bore, and a notch in it, to help fluid flow thru the drainback port. Don't forget to also drill this port out to 5/16", before you press the new bushing in. ...and installed I used special hose clamps to align the two pump halves to bolt it back together. Its important it goes back together perfectly as it came apart or you will wreck the pump and then the trans. I scribed the two halves before I split it, to make sure it was perfect. Pump reinstalled in its home. My solenoid pack was leaking ATF thru the connector, so I swapped it out for the OEM pack from the parts truck's E4OD And whats this? Why, it appears to be a valve body from Punisher Valve Bodies! His kits are super easy to install, only took like 5 minutes with the trans already out. From there I added a new trans pan from Dorman (complete with drain plug), new filter, and reinstalled the trans! That said, I finally got it back on the road Thursday afternoon, so ive only driven it about 75 miles, but DAMN. This thing shifts nice now. Ill have to give it a few more miles for the PCM to learn the trans, but it really does shift like a dream now. There is a great article covering the full E4OD rebuild over on Four Door Broncos which i referenced while doing this, you can check it out here. So last week, I was rummaging around at the scrap steel yard, when I found the perfect piece of steel: As soon as I saw it, I knew what to use it for: the tire carrier! So, drill 4 holes, 21/32", and then install 3 studs, used for a Sterling 10.25 Cut the two bottom studs off the stock tire carrier, knock the top one out, and drill that hole out to 21/32" as well. Then, press the 4td stud thru both the stock mount, and the new plate. Then weld top and bottom to the tire carrier and viola! 8-lug tire carrier! |
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